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I found a couple more problems when testing all the limits. When I took the gantry to X maximum, the dust collector hose pulled off! I put it back on, but I'm not sure how stable this is. Also, when I originally set the Y maximum and minimum, I wanted as much spindle travel as possible. But it appears that if you're at the Y max and move in the X direction, you can hit the middle support with the dust collector boot. We've got several inches Y travel beyond the nominal 48", so we may want to look into reducing this to clear the supports.
 
I found a couple more problems when testing all the limits. When I took the gantry to X maximum, the dust collector hose pulled off! I put it back on, but I'm not sure how stable this is. Also, when I originally set the Y maximum and minimum, I wanted as much spindle travel as possible. But it appears that if you're at the Y max and move in the X direction, you can hit the middle support with the dust collector boot. We've got several inches Y travel beyond the nominal 48", so we may want to look into reducing this to clear the supports.
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== Resources ==
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[[File:ShopBot PSOne Post Processors.zip|ShopBot PSOne Post Processors.zip]] - Post Processors for Vectric Aspire and VCarve Pro 8.0 which include the change to check that the spindle actually started.
    
[[Category:Fabrication]]
 
[[Category:Fabrication]]
 
[[Category:CNC]]
 
[[Category:CNC]]
 
[[Category:Future Things Bus Data Sources]]
 
[[Category:Future Things Bus Data Sources]]
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